Strange play has developed in the drive side crank arm of my converted-to-ss commuter in the last couple of days. Bolt wasn’t moving so wasn’t immediately concerned. Tonight I’ve removed the arm, getting the bolt out was hard but didn’t need the puller to get the arm off, just wiggled and pulled. BB looks ok in itself (had visions of slightly bent axle) but after cleaning everything and sticking it back on, the bolt now won’t tighten.
If I’ve threaded the bb, guess i need to replace it (bolt looks ok) but could the square hole in the crank arm be damaged?