Ok so in no particular orders:
I have removed the injectors, the paper gasket was quite “greasy”, so I used blue gasket paste to put it back together, I have changed the breather that goes from the manifold, under the injector to the top of the airbox and made sure all was cleaned (it was indeed a bit jammed).
Idling motor works just fine.
Chris are you talking about removing the whole injector?
Now the new thing is the exhaust fume being very white.
I’ll pop by the mechanic see if he has an idea. Otherwise I just hope I’ll be able to get to my new work (starting on monday) without too much issues.