So I have a set of 2010 fox float 36 forks, Last year I got some old stock stanchions from Mojo with a 1.5in steerer for £50. Works absolutely brilliantly on my Intense tracer 2.
Unfortunately the internals have always been a bit flaky, the old school none-inverted FIT damper blows up like a balloon and becomes more like a spring and the air piston has the common issue of letting all the fork oil into the air chamber.
So the fork doesn’t really work very well – but I didn’t want to change it because I love the chassis as it is and you can’t get the 1.5in sheerer standard anymore. Also I can’t afford (or want) to change my headset and stem as well as forks.
So I found an inverted FIT damper on ebay for £100. No problems there as it’s the one they made to retrofit onto pre 2011 forks (they have changed the threads on the uppers)
I also found a 2014 air spring and negative plate for £60. This I was less sure about but I thought for the price I would take a punt.
Bugger – I’d forgotten this; Fox increased the internal diameter of their stanchions (probably to save weight) and neither the spring nor the plate will fit inside.
Instead of doing the sensible thing at this point and trying to return the parts I thought sod it – lets get the electric sander out and see if we can MAKE them fit.
So took off the scraper seals (noticing they seemed identical in diameter to the one from the original spring) – clamped the sander in a vice and slowly turned the air piston to remove material. Eventually got the piston to slide inside the stanchion using the old piston as a guide to how much play there should be. After putting the scraper seals back in I did notice a fair bit more stiction than the old piston but then there are double the number of seals…?
Followed a similar process to make the negative plate fit – put it all back together, pumped it up and discovered I only had 150mm of travel. No problem. Disassemble and cut 10mm off the shuttle bumper with some scissors. Voila – 160mm.
Round the block test feels pretty good, although I am now wondering whether I should have removed some material from the piston behind the scraper seals. This may account for the increased stiction.
Anyway I will take it for a spin this afternoon and see what happens.